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authorCristian Ciocaltea <[email protected]>2023-12-20 23:17:41 +0200
committerConor Dooley <[email protected]>2024-01-31 12:23:26 +0000
commite16d3dc0a2d7cd7bd673ce08b39a4239aafe0938 (patch)
treed5175be6a495bd8e680eeb36995cc1037e56a6bc /tools/perf/scripts/python/Perf-Trace-Util
parent6e204aa2116cf9677b8b93ba15d7831d98e4a236 (diff)
riscv: dts: starfive: visionfive-v1: Setup ethernet phy
The StarFive VisionFive V1 SBC uses a Motorcomm YT8521 PHY supporting RGMII-ID, but requires manual adjustment of the RX internal delay to work properly. The default RX delay provided by the driver is 1.95 ns, which proves to be too high. Applying a 50% reduction seems to mitigate the issue. Also note this adjustment is not necessary on BeagleV Starlight SBC, which uses a Microchip PHY. Hence, there is no indication of a misbehaviour on the GMAC side, but most likely the issue stems from the Motorcomm PHY. While at it, drop the redundant gpio include, which is already provided by jh7100-common.dtsi. Co-developed-by: Emil Renner Berthing <[email protected]> Signed-off-by: Emil Renner Berthing <[email protected]> Signed-off-by: Cristian Ciocaltea <[email protected]> Reviewed-by: Jacob Keller <[email protected]> Reviewed-by: Andrew Lunn <[email protected]> Reviewed-by: Emil Renner Berthing <[email protected]> Signed-off-by: Conor Dooley <[email protected]>
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