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When the HCD is disconnected, the DMA transfers still in-flight were cleaned-up
but the count of available DMA channels (e.g. available_host_channels) was not
reset.
The pool of DMA channels can be depleted when doing unclean
disconnection of USB peripherals, and reaches the point where no
transfer was possible until the next reboot/reload of the driver.
Tested by putting a programmable USB mux on the port and randomly
plugging/unpluging a USB HUB with USB mass-storage key, USB-audio and
USB-ethernet dongle connected to its downstream ports, and also doing the
disconnection early while the devices are still enumerating to get more URBs
in-flight.
After the patch, the devices are still enumerating after thousands of cycles,
while the port was totally dead before.
Signed-off-by: Vincent Palatin <[email protected]>
Acked-by: John Youn <[email protected]>
Signed-off-by: Felipe Balbi <[email protected]>
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The misc subsystem (which is used for /dev/fuse) initializes private_data to
point to the misc device when a driver has registered a custom open file
operation, and initializes it to NULL when a custom open file operation has
*not* been provided.
This subtle quirk is confusing, to the point where kernel code registers
*empty* file open operations to have private_data point to the misc device
structure. And it leads to bugs, where the addition or removal of a custom open
file operation surprisingly changes the initial contents of a file's
private_data structure.
So to simplify things in the misc subsystem, a patch [1] has been proposed to
*always* set the private_data to point to the misc device, instead of only
doing this when a custom open file operation has been registered.
But before this patch can be applied we need to modify drivers that make the
assumption that a misc device file's private_data is initialized to NULL
because they didn't register a custom open file operation, so they don't rely
on this assumption anymore. FUSE uses private_data to store the fuse_conn and
errors out if this is not initialized to NULL at mount time.
Hence, we now set a file's private_data to NULL explicitly, to be independent
of whatever value the misc subsystem initializes it to by default.
[1] https://lkml.org/lkml/2014/12/4/939
Reported-by: Giedrius Statkevicius <[email protected]>
Reported-by: Thierry Reding <[email protected]>
Signed-off-by: Tom Van Braeckel <[email protected]>
Signed-off-by: Miklos Szeredi <[email protected]>
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This reverts commit 2fa645cb2703d9b3786d850db815414dfeefa51d.
The assumption that at least 1 preferred console will be registered
when the stdout-path property is set is invalid, which can result
in _no_ consoles.
Signed-off-by: Peter Hurley <[email protected]>
Signed-off-by: Rob Herring <[email protected]>
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Commit 106937e8ccdc ("of: fix handling of '/' in options for
of_find_node_by_path()") caused a regression in OF handling of
stdout-path. While it fixes some cases which have '/' after the ':', it
breaks cases where there is more than one '/' *before* the ':'.
For example, it breaks this boot string
stdout-path = "/rdb/serial@f040ab00:115200";
So rather than doing sequentialized checks (first for '/', then for ':';
or vice versa), to get the correct behavior we need to check for the
first occurrence of either one of them.
It so happens that the handy strcspn() helper can do just that.
Fixes: 106937e8ccdc ("of: fix handling of '/' in options for of_find_node_by_path()")
Signed-off-by: Brian Norris <[email protected]>
Cc: [email protected] # 3.19
Acked-by: Leif Lindholm <[email protected]>
Signed-off-by: Rob Herring <[email protected]>
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There were regressions seen with commit 106937e8ccdc ("of: fix handling
of '/' in options for of_find_node_by_path()"), where we couldn't handle
extra '/' before the ':'. Let's test for this now.
Confirmed that this test fails without the previous patch and passes
when patched. All other tests pass.
Signed-off-by: Brian Norris <[email protected]>
Acked-by: Leif Lindholm <[email protected]>
Signed-off-by: Rob Herring <[email protected]>
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The error code paths that require cleanup use a goto to jump to the
cleanup code and return an error code. However, the error code variable
res, which is initialized to -EINVAL when declared, is then overwritten
with the return value of of_parse_phandle_with_args(), and reused as the
return code from of_irq_parse_one(). This leads to an undetermined error
being returned instead of the expected -EINVAL value. Fix it.
Signed-off-by: Laurent Pinchart <[email protected]>
Cc: [email protected] # 3.13+
Signed-off-by: Rob Herring <[email protected]>
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The current error-path code (when gpiod_get_index() reports
an error) can never free pwrseq->reset_gpios[0], but might
try to tree pwrseq->reset_gpios[-1], which has unfortunate
consequences.
Signed-off-by: NeilBrown <[email protected]>
Fixes: 934f1f48330ed695927a51fa068dc5d673f2da19
Acked-by: Javier Martinez Canillas <[email protected]>
Signed-off-by: Ulf Hansson <[email protected]>
Reported-by: Srinivas Kandagatla <[email protected]>
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into drm-fixes
single radeon fix.
* 'drm-fixes-4.0' of git://people.freedesktop.org/~agd5f/linux:
drm/radeon: drop ttm two ended allocation
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git://git.kernel.org/pub/scm/linux/kernel/git/daeinki/drm-exynos into drm-fixes
Some urgent regression fixes to booting failures Exynos DRM occured.
Summary:
- Fix two urgent null pointer dereference bugs in case of enabling
or disabling IOMMU. There was two cases to these issues.
One is that plane->crtc is accessed by exynos_disable_plane()
when device tree binding is broken so device driver tries
to release, which means that the mode set operation isn't invoked yet
so plane->crtc is still NULL and exynos_disable_plane() will access
NULL pointer. This issue is fixed by checking if the plane->crtc
is NULL or not in exynos_disable_plane()
Other is that fimd_wait_for_vblank() is called to avoid from page fault
with IOMMU before the ctx object is created. At this time,
fimd_wait_for_vblank() tries to access ctx->crtc but the ctx->crtc
is still NULL because exynos_drm_crtc_create() isn't called yet.
This issue is fixed by creating a crtc object and setting it to
ctx->crtc prior to fimd_wait_for_vblank() call.
For more details, you can refer to below an e-mail thread,
http://www.spinics.net/lists/linux-samsung-soc/msg42436.html
- Remove unnecessary file not used and fix trivial issues.
* 'exynos-drm-fixes' of git://git.kernel.org/pub/scm/linux/kernel/git/daeinki/drm-exynos:
drm/exynos: fix the initialization order in FIMD
drm/exynos: fix typo config name correctly.
drm/exynos: Check for NULL dereference of crtc
drm/exynos: IS_ERR() vs NULL bug
drm/exynos: remove unused files
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Use jiffies_to_msecs for converting jiffies as it handles all of the corner
cases reliably and also helps readability. The printk format is fixed up
as jiffies_to_msecs returns unsigned int not unsigned long.
Signed-off-by: Nicholas Mc Guire <[email protected]>
Signed-off-by: David S. Miller <[email protected]>
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This reverts commit 11ad714b98f6d9ca0067568442afe3e70eb94845 because
it breaks cx82310_eth.
The custom USB_DEVICE_CLASS macro matches
bDeviceClass, bDeviceSubClass and bDeviceProtocol
but the common USB_DEVICE_AND_INTERFACE_INFO matches
bInterfaceClass, bInterfaceSubClass and bInterfaceProtocol instead, which are
not specified.
Signed-off-by: Ondrej Zary <[email protected]>
Signed-off-by: David S. Miller <[email protected]>
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/proc/kcore investigates the "System RAM" elements in /proc/iomem to
initialize it's memory tables. Therefore we have to register them
before it tries to do so. kcore uses device_initcall() so let's
use arch_initcall() for the registry.
Also we need ARCH_PROC_KCORE_TEXT to get the virtual addresses of
the kernel image correct.
Reported-by: David Ahern <[email protected]>
Signed-off-by: David S. Miller <[email protected]>
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Or Gerlitz says:
====================
mlx4 driver fixes for 4.0-rc
Just few small fixes for the 4.0 rc cycle.
The fix from Moni addresses an issue from 4.0-rc1 so we
just need it for net.
Eran's fix for off-by-one should go to 3.19.y too.
====================
Signed-off-by: David S. Miller <[email protected]>
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Port statistics bitmap will now be initialized at port init. Even before
starting the port, statistics are visible to the user and must be properly masked.
Signed-off-by: Eran Ben Elisha <[email protected]>
Signed-off-by: Hadar Hen Zion <[email protected]>
Signed-off-by: Or Gerlitz <[email protected]>
Signed-off-by: David S. Miller <[email protected]>
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For RoCE ports, we set the u32 PMA values based on u64 HCA counters. In case of
overflow, according to the IB spec, we have to saturate a counter to its
max value, do that.
Fixes: c37791349cc7 ('IB/mlx4: Support PMA counters for IBoE')
Signed-off-by: Majd Dibbiny <[email protected]>
Signed-off-by: Eran Ben Elisha <[email protected]>
Signed-off-by: Hadar Hen Zion <[email protected]>
Signed-off-by: Or Gerlitz <[email protected]>
Signed-off-by: David S. Miller <[email protected]>
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NUM_PORT_STATS was 9 instead of 10, which caused off-by-one bug when
displaying the statistics starting from tx_chksum_offload in ethtool.
Fixes: f8c6455bb04b ('net/mlx4_en: Extend checksum offloading by CHECKSUM COMPLETE')
Signed-off-by: Eran Ben Elisha <[email protected]>
Signed-off-by: Hadar Hen Zion <[email protected]>
Signed-off-by: Or Gerlitz <[email protected]>
Signed-off-by: David S. Miller <[email protected]>
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Processing an event is done in a different context from the one when
the event was dispatched. This requires a check that the slave
net device is still valid when the event is being processed. The check is done
under the iboe lock which ensure correctness.
Fixes: a57500903093 ('IB/mlx4: Add port aggregation support')
Signed-off-by: Moni Shoua <[email protected]>
Signed-off-by: Or Gerlitz <[email protected]>
Signed-off-by: David S. Miller <[email protected]>
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git://git.kernel.org/pub/scm/linux/kernel/git/tiwai/sound
Pull sound fixes from Takashi Iwai:
"This is a collection of many small fixes. Most of fixes are for ASoC
drivers, including the fixes of wrong field usages for boolean kctls.
In addition, there is a fix in ASoC core for adding proper locks for
component lists, and a fix for a HD-audio regression by the previous
mono channel fix"
* tag 'sound-4.0-rc5' of git://git.kernel.org/pub/scm/linux/kernel/git/tiwai/sound: (24 commits)
ALSA: hda - Treat stereo-to-mono mix properly
ASoC: wm9713: Fix wrong value references for boolean kctl
ASoC: wm9712: Fix wrong value references for boolean kctl
ASoC: wm8960: Fix wrong value references for boolean kctl
ASoC: wm8955: Fix wrong value references for boolean kctl
ASoC: wm8904: Fix wrong value references for boolean kctl
ASoC: wm8903: Fix wrong value references for boolean kctl
ASoC: wm8731: Fix wrong value references for boolean kctl
ASoC: wm2000: Fix wrong value references for boolean kctl
ASoC: tas5086: Fix wrong value references for boolean kctl
ASoC: pcm1681: Fix wrong value references for boolean kctl
ASoC: es8238: Fix wrong value references for boolean kctl
ASoC: cs4271: Fix wrong value references for boolean kctl
ASoC: ak4641: Fix wrong value references for boolean kctl
ASoC: adav80x: Fix wrong value references for boolean kctl
ASoC: Fix component lists locking
ASoC: Intel: remove conflicts when load/unload multiple firmware images
ASoC: rt286: Change the DMI mapping for Dino
ASoC: sgtl5000: remove useless register write clearing CHRGPUMP_POWERUP
ASoC: fsl_ssi: Don't try to round-up for PM divisor calculation
...
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Pull crypto fixes from Herbert Xu:
"Fix a bug in the ARM XTS implementation that can cause failures in
decrypting encrypted disks, and fix is a memory overwrite bug that can
cause a crash which can be triggered from userspace"
* git://git.kernel.org/pub/scm/linux/kernel/git/herbert/crypto-2.6:
crypto: aesni - fix memory usage in GCM decryption
crypto: arm/aes update NEON AES module to latest OpenSSL version
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git://git.kernel.org/pub/scm/linux/kernel/git/jikos/livepatching
Pull livepatching fix from Jiri Kosina:
- fix for potential race with module loading, from Petr Mladek.
The race is very unlikely to be seen in real world and has been found
by code inspection, but should be fixed for 4.0 anyway.
* 'for-linus' of git://git.kernel.org/pub/scm/linux/kernel/git/jikos/livepatching:
livepatch: Fix subtle race with coming and going modules
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git://git.kernel.org/pub/scm/linux/kernel/git/jikos/hid
Pull HID fixes from Jiri Kosina:
- fixes for pen pen proximity / touch events in wacom driver, from Ping
Cheng and Benjamin Tissoires
- two new device-specific quirks from Oliver Neukum and Forest
Wilkinson
* 'for-linus' of git://git.kernel.org/pub/scm/linux/kernel/git/jikos/hid:
HID: wacom: check for wacom->shared before following the pointer
HID: tivo: enable all buttons on the TiVo Slide Pro remote
HID: add ALWAYS_POLL quirk for a Logitech 0xc007
HID: wacom: rely on actual touch down count to decide touch_down
HID: wacom: do not send pen events before touch is up/forced out
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This code is no longer used now that mach-msm has been removed.
Delete it.
Cc: Felipe Balbi <[email protected]>
Cc: Greg Kroah-Hartman <[email protected]>
Cc: [email protected]
Cc: David Brown <[email protected]>
Cc: Bryan Huntsman <[email protected]>
Cc: Daniel Walker <[email protected]>
Signed-off-by: Stephen Boyd <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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This dependency no longer exists now that mach-msm has been
removed. Delete it.
Cc: Greg Kroah-Hartman <[email protected]>
Cc: Alan Stern <[email protected]>
Cc: [email protected]
Cc: David Brown <[email protected]>
Cc: Bryan Huntsman <[email protected]>
Cc: Daniel Walker <[email protected]>
Signed-off-by: Stephen Boyd <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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There are currently no umc drivers implementing suspend/resume, so remove
the legacy suspend/resume support from the framework. If a umc driver ever
wants to implement suspend/resume they can use dev_pm_ops, which works out
of the box without any additional support necessary from the bus itself.
Signed-off-by: Lars-Peter Clausen <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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of_device_id is always used as const.
(See driver.of_match_table and open firmware functions)
Signed-off-by: Fabian Frederick <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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As per the SAF1761 data sheet[0], the DcChipID register represents
the hardware version number (0001h) and the chip ID (1582h) for the
Peripheral Controller.
However as per the ISP1761 data sheet[1], the DcChipID register
represents the hardware version number (0015h) and the chip ID (8210h)
for the Peripheral Controller.
This patch adds support for both the chip ID values.
[0] http://www.nxp.com/documents/data_sheet/SAF1761.pdf
[1] http://pdf.datasheetcatalog.com/datasheets2/74/742102_1.pdf
Cc: Felipe Balbi <[email protected]>
Signed-off-by: Sudeep Holla <[email protected]>
Acked-by: Laurent Pinchart <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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Use spin_{un,}lock_irq{save,restore} in isp1760_udc_{start,stop} to
prevent following potentially deadlock scenario between
isp1760_udc_{start,stop} and isp1760_udc_irq :
=================================
[ INFO: inconsistent lock state ]
4.0.0-rc2-00004-gf7bb2ef60173 #51 Not tainted
---------------------------------
inconsistent {HARDIRQ-ON-W} -> {IN-HARDIRQ-W} usage.
in:imklog/2118 [HC1[1]:SC0[0]:HE0:SE1] takes:
(&(&udc->lock)->rlock){?.+...}, at: [<c0397a93>] isp1760_udc_irq+0x367/0x9dc
{HARDIRQ-ON-W} state was registered at:
[<c05135b3>] _raw_spin_lock+0x23/0x30
[<c0396b87>] isp1760_udc_start+0x23/0xf8
[<c039dc21>] udc_bind_to_driver+0x71/0xb0
[<c039de4f>] usb_gadget_probe_driver+0x53/0x9c
[<bf80d0df>] usb_composite_probe+0x8a/0xa4 [libcomposite]
[<bf8311a7>] 0xbf8311a7
[<c00088c5>] do_one_initcall+0x8d/0x17c
[<c050b92d>] do_init_module+0x49/0x148
[<c0087323>] load_module+0xb7f/0xbc4
[<c0087471>] SyS_finit_module+0x51/0x74
[<c000d8c1>] ret_fast_syscall+0x1/0x68
irq event stamp: 4966
hardirqs last enabled at (4965): [<c05137df>] _raw_spin_unlock_irq+0x1f/0x24
hardirqs last disabled at (4966): [<c00110b3>] __irq_svc+0x33/0x64
softirqs last enabled at (4458): [<c0023475>] __do_softirq+0x23d/0x2d0
softirqs last disabled at (4389): [<c002380b>] irq_exit+0xef/0x15c
other info that might help us debug this:
Possible unsafe locking scenario:
CPU0
----
lock(&(&udc->lock)->rlock);
<Interrupt>
lock(&(&udc->lock)->rlock);
*** DEADLOCK ***
1 lock held by in:imklog/2118:
#0: (&f->f_pos_lock){+.+.+.}, at: [<c010a101>] __fdget_pos+0x31/0x34
Signed-off-by: Sudeep Holla <[email protected]>
Cc: Laurent Pinchart <[email protected]>
Cc: Greg Kroah-Hartman <[email protected]>
Cc: Felipe Balbi <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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USB PHY works proper is the base for the coming USB controller operation.
With this patch, it can avoid the controller drivers which are linked
earlier than USB PHY always being probed deferral.
Look at drivers/Makefile, it links phy first with the similar method.
Signed-off-by: Zhangfei Gao <[email protected]>
Acked-by: Peter Chen <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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Change 'Supsend' to 'Suspend'
Signed-off-by: Yannick Guerrini <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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Ensure that clients can automatically configure themselves and avoid a
nasty warning at boot by providing capability information.
Signed-off-by: Mark Brown <[email protected]>
Signed-off-by: Vinod Koul <[email protected]>
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Fixes errors thrown by checkpatch over a space issue and the
incorrect indentation of a switch statement.
Signed-off-by: Bas Peters <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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declarations
This patch places braces on a new line following function declarations.
Signed-off-by: Bas Peters <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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Instead of manual device_create_file() and device_remove_file() calls,
assign the static attribute groups to the lun device to register.
The RO or RW permissions for some entries are decided in is_visible
callback. This simplifies the code (also the logic) and avoids the
possible races, too.
Signed-off-by: Takashi Iwai <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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The backlight_device_unregister() function tests whether its argument is NULL
and then returns immediately. Thus the test around the call is not needed.
This issue was detected by using the Coccinelle software.
Signed-off-by: Markus Elfring <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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"release_firmware"
The release_firmware() function tests whether its argument is NULL and then
returns immediately. Thus the test around the call is not needed.
This issue was detected by using the Coccinelle software.
Signed-off-by: Markus Elfring <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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"usb_put_hcd"
The usb_put_hcd() function tests whether its argument is NULL and then
returns immediately. Thus the test around the call is not needed.
This issue was detected by using the Coccinelle software.
Signed-off-by: Markus Elfring <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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"umc_device_unregister"
The umc_device_unregister() function tests whether its argument is NULL
and then returns immediately. Thus the test around the call is not needed.
This issue was detected by using the Coccinelle software.
Signed-off-by: Markus Elfring <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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The Marvell Armada 385 AP needs a dumb phy in order to enable the USB3 VBUS.
Add a call to retrieve a USB PHY to XHCI plat in order to support this.
Signed-off-by: Maxime Ripard <[email protected]>
Signed-off-by: Mathias Nyman <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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Some toggling operation in xHCI driver still use conditional toggling:
ring->cycle_state = (ring->cycle_state ? 0 : 1);
Use XOR to invert the cycle state instead of a conditional toggle to unify
cycle state toggling operation in xHCI driver.
Signed-off-by: Lin Wang <[email protected]>
Signed-off-by: Mathias Nyman <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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This is only an API consolidation and should make things more readable
it replaces var * HZ / 1000 by msecs_to_jiffies(var).
Signed-off-by: Nicholas Mc Guire <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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This is only an API consolidation and should make things more readable
it replaces var * HZ / 1000 by msecs_to_jiffies(var).
Signed-off-by: Nicholas Mc Guire <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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this patch fixes following sparse warning:
sl811-hcd.c:1804:24: warning: symbol 'sl811h_driver' was not declared. Should it be static?
Signed-off-by: Lad, Prabhakar <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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This patch adds runtime power management support for otg fsm mode, since
A-device in a_idle state cannot detect data pulse irq after suspended, here
enable wakeup by connection before suspend to make it can be resumed by DP;
and handle wakeup from that state like SRP.
Signed-off-by: Li Jun <[email protected]>
Signed-off-by: Peter Chen <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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If CI_HDRC_TURN_VBUS_EARLY_ON is set, turn on vbus before adding hcd, so it
will not set reg_vbus of ehci_ci_priv, then vbus will not be handled by ehci core.
Signed-off-by: Li Jun <[email protected]>
Signed-off-by: Peter Chen <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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Some usb PHYs need power supply from vbus to make it work, eg mxs-phy, if
there is no vbus, USB PHY will not in correct state when the controller starts
to work, for host, this requires vbus should be turned on before setting port
power(PP) of ehci, to work with this kind of USB PHY design, this patch adds
a flag CI_HDRC_TURN_VBUS_EARLY_ON, can be checked by host driver to turn on
vbus while start host.
Signed-off-by: Li Jun <[email protected]>
Signed-off-by: Peter Chen <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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Since PHY for ChipIdea is optional (not all SoCs having PHY for ChipIdea should
be programmed), we register 'nop' PHY for platforms that do not have
programmable PHY.
Acked-by: Felipe Balbi <[email protected]>
Signed-off-by: Andy Shevchenko <[email protected]>
Signed-off-by: Peter Chen <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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For chipidea, its resume sequence is not-EHCI compatible, see
below description for FPR at portsc. So in order to send SoF in
time for remote wakeup sequence(within 3ms), the RUN/STOP bit must
be set before the resume signal is ended, but the usb resume
code may run after resume signal is ended, so we had to set it
at suspend path.
Force Port Resume - RW. Default = 0b.
1= Resume detected/driven on port.
0=No resume (K-state) detected/driven on port.
Host mode:
Software sets this bit to one to drive resume signaling. The Controller sets this bit to '1' if
a J-to-K transition is detected while the port is in the Suspend state. When this bit
transitions to a '1' because a J-to-K transition is detected, the Port Change Detect bit in
the USBSTS register is also set to '1'. This bit will automatically change to '0' after the
resume sequence is complete. This behavior is different from EHCI where the controller
driver is required to set this bit to a '0' after the resume duration is timed in the driver.
Note that when the controller owns the port, the resume sequence follows the defined
sequence documented in the USB Specification Revision 2.0. The resume signaling
(Full-speed 'K') is driven on the port as long as this bit remains a '1'. This bit will remain
a '1' until the port has switched to idle. Writing a '0' has no affect because the port
controller will time the resume operation, clear the bit and the port control state switches
to HS or FS idle.
This field is '0' if Port Power(PP) is '0' in host mode.
This bit is not-EHCI compatible.
Acked-by: Alan Stern <[email protected]>
Signed-off-by: Peter Chen <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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CI_HDRC_FORCE_FULLSPEED is set in the platform data
PORTSC_PFSC is not set on entering host mode which means the USB OTG
controller will attempt to enumerate USB devices at high speed even when the
CI_HDRC_FORCE_FULLSPEED flag is set in the platform data.
This patch ensures it is set right before host mode operations begin if needed.
Signed-off-by: Daniel Tang <[email protected]>
Signed-off-by: Peter Chen <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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connect at full speed
Signed-off-by: Daniel Tang <[email protected]>
Signed-off-by: Peter Chen <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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At chipidea revision 2.40a, there is a below errata:
9000531823 B2-Medium Adding a dTD to a Primed Endpoint May Not Get Recognized
Title: Adding a dTD to a Primed Endpoint May Not Get Recognized
Impacted Configuration: All device mode configurations.
Description:
There is an issue with the add dTD tripwire semaphore (ATDTW bit in USBCMD register)
that can cause the controller to ignore a dTD that is added to a primed endpoint.
When this happens, the software can read the tripwire bit and the status bit at '1'
even though the endpoint is unprimed.
After executing a dTD, the device controller endpoint state machine executes a final
read of the dTD terminate bit to check if the application added a dTD to the linked
list at the last moment. This read is done in the finpkt_read_latest_next_td (44) state.
After the read is performed, if the terminate bit is still set, the state machine moves
to unprime the endpoint. The decision to unprime the endpoint is done in the
checkqh_decision (59) state, based on the value of the terminate bit.
Before reaching the checkqh_decision state, the state machine traverses the
writeqhtd_status (57), writeqh_status (56), and release_prime_mask (42) states.
As shown in the waveform, the ep_addtd_tripwire_clr signal is not set to clear
the tripwire bit in these states.
Workaround:
The software must implement a periodic poll cycle, and check for each dTD
pending on execution (Active = 1), if the enpoint is primed. It can do this by reading
the corresponding bits in the ENDPTPRIME and ENDPTSTAT registers. If these bits are
read at 0, the software needs to re-prime the endpoint by writing 1 to the corresponding
bit in the ENDPTPRIME register. This can be done for every microframe, every frame or
with a larger interval, depending on the urgency of transfer execution for the application.
Tested-by: Stefan Agner <[email protected]>
Signed-off-by: Peter Chen <[email protected]>
Signed-off-by: Sanchayan Maity <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>
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